Previously ..….
Conway Stewart pressure bars are secured by a pass-through screw at the end of the barrel as opposed to the floating pressures used by Parker in the Duofold. The screw was easily removed freeing the remaining portion of the pressure bar. Now for the bad news, replacement bars based on the Conway Stewart design are not available as an after-market replacement part.
As a side note, the back of the Conway Stewart pressure bar base is a patent number. Yes, I researched the GB patent and would never have guessed the patent diagrams supported this pressure bar.
Time for bright ideas. As I see it I have three; 1) repair the existing pressure bar, 2) modify a replacement pressure bar, or 3) install a floating pressure bar.
Conway Stewart’s design is a three-part pressure bar, a base that is held in place by a screw, with an attached pressure bar similar to a floating bar found in a Duofold. As I was preparing the base for a bright idea I discovered the residual of the pressure bar was attached to the base by tabs.
New Pressure Bar
This discovery changed everything, now I can apply all three bright ideas simultaneously. Prior to removing the damaged pressure bar, I placed a preemptive order for a replacement floating pressure bar. Why not use the original base and attach the new floating pressure bar? I notched the back of the floating pressure bar as it was a smidge larger than the base. Applied crazy/super glue, placed the floating pressure bar so the tab fit in the notch, and folded the tab over securing the two.
Now fully assembled, would it stand up to pressure? YES IT DID. I put the new mechanism through 20 pressure tests and it performed perfectly. Time to look at the barrel.
The barrel is warped, and the outside diameter varies by 1mm at random locations. I tried using a drill to reduce the discrepancies but it didn’t work so I applied a small circular file – perfect. Now the base mounting ring easily slides the length of the barrel.
Installation
Time to clean the mounting threads and screw. Scrubbed and brush the threads but the mounting screw still felt obstructed. I applied silicon grease to the threads. The screw twisted freely without binding. Time to put it together.
I wanted to ensure the new bar would hug the barrel wall so I bent the mounting ring upward making a 120-degree angle. I inserted a piece of electrical wire insulation threw the mounting screw to hold the screw steady and in place.
The bar fit into place perfectly, inserted a screwdriver, and started securing the mounting screw. The notch in the mounting screw is shallow. The screwdriver popped out multiple times catching on the pressure bar. This caused my well-intended bend to go to Hell. The new bar no longer hugs the wall of the barrel, now it is an obstruction impairing the ink sac.
Opting for the lesser of two evils (which is still evil), I left the new pressure bar as an obstruction. The next problem is the pressure button. The old pressure bar had a short fixture on which to mount the pressure button. This was affected by a bend in the pressure bar near the mounting ring. My new mechanism also has a bend but at a different location; therefore, the push button didn’t push.
The solution is obvious – large gauge speaker wire. I simply cut an inch of wire and removed the insulation. You see speaker wire is flexible and easy to work with. The idea is simple, trim the insulation to size and use it to artificially extend the pressure button to the new bend, thus the pressure button will push.
Does the Push button Push? Did the ink sac fill? Do I have inky fingers?
I inserted the nib into a bottle of 4001 black and depressed the push button… bubbles. Repeated the process until the bubbles stopped. Judge for yourself and no inky fingers.
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